Salinas River Cogeneration Company - Executive Summary

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EXECUTIVE SUMMARY 
 
 
Accidental Release Prevention and Emergency Response Policies 
 
Salinas River Cogeneration Company stores and utilizes anhydrous ammonia in  
a selective catalytic reduction (SCR) process at their facility in the San Ardo oil  
fields near Paso Robles, California.  It is Salinas River Cogeneration Company's  
policy to comply with all applicable governmental regulations.  Further, it is  
Salinas River Cogeneration Company's objective to be a responsible citizen of  
the community in all of its business activities. 
 
Salinas River Cogeneration Company emphasizes safe and environmentally  
sound operating practices and procedures through their employee training  
programs.  In addition to job specific training, operators and maintenance  
personnel receive training in fire prevention, fire control, accident prevention,  
safety, and first aid.  Additionally, an emergency action plan has been prepared  
for Salinas River Cogeneration Company and a chain of command to respond to  
 
emergencies has been established. 
 
Salinas River Cogeneration Company has developed a detailed Compliance  
Audit Checklist which is used to evaluate compliance with the Process Safety  
Management (PSM) standard and 40 CFR Part 68 (RMP regulations).  At least  
every three years, Salinas River Cogeneration Company audits these programs  
and any findings of noncompliance are documented and responded to and the  
deficiencies are corrected. 
 
Description of the Stationary Source and Regulated Substances  
 
Texaco Yoakum Energy Company, a wholly-owned subsidiary of Texaco  
Producing Inc., formed a general partnership with the Anacapa Energy  
Company, a wholly-owned subsidiary of Edison Mission Energy Company, for  
the development of the cogeneration plant.  The partnership, named Salinas  
River Cogeneration Company, owns and operates the facility.  The plant began  
commercial operation in October, 1991.   
 
The Salinas River Cogeneration Company facility is located in Section 2,  
T32S/R10E, MDB 
&M in the sparsely populated San Ardo oil fields. 
 
Cogeneration, in the case of the Salinas River project, is the simultaneous  
production of thermal energy and electrical energy from the combustion of a  
single fuel source.  Combustion of the fuel takes place in a gas turbine that is  
physically coupled to an electric generator.  Waste heat from the gas turbine's  
exhaust flows into a heat recovery steam generator (HRSG).  The HRSG  
extracts the heat from the exhaust gases and produces steam for thermally  
enhanced oil recovery.  Electricity is produced at the same time via the electric  
generator coupled to the combustion turbine.   
 
Anhydrous ammonia is used at the Salinas River Cogeneration Company facility  
to create a reducing atmosphere in the selective catalytic reduction (SCR)  
process.  This reducing atmosphere in the flue gas helps convert nitrogen oxides  
to nitrogen and water as it passes through the catalytic reactor.  The operation of  
the SCR system substantially lowers 
the emissions of nitrogen oxides from the  
gas turbine. 
 
Liquid ammonia is stored in a 15,000 gallon (water capacity) storage tank.  The  
maximum intended inventory of the anhydrous ammonia storage tank is based  
on the American National Standard Institute's K61.1 safety requirements and the  
Occupational Safety and Health Administration (OSHA) regulations published in  
Section 1910.111 of 29 CFR (and Section 509 of Title 8, CCR).  These standards  
and regulations limit the maximum ammonia storage capacity of the tank to  
approximately 69,960 pounds. 
 
For purposes of the offsite consequence analyses, the RMP regulations define  
the toxic endpoint for anhydrous ammonia as 0.14 mg/l (200 ppm).  This  
concentration has been established by the American Industrial Hygiene  
Association as the Emergency Response Planning Guideline Level 2 (ERPG-2).   
 
ERPG-2 is the maximum airborne concentration below which it is believed that  
nearly all individuals could be exposed for up to one hour witho 
ut experiencing or  
developing irreversible or other serious health effects or symptoms which could  
impair an individual's ability to take protective action. 
 
Worst-Case Release Scenario and Alternative Release Scenario 
 
Offsite consequence analyses are used as tools to assist in emergency response  
planning.  The RMP regulations require the owner or operator of a stationary  
source to analyze the offsite impacts due to an accidental release of a regulated  
substance.  The offsite consequence analysis for a Program 3 process must  
analyze the worst-case release scenario and an alternative release scenario.   
Since Salinas River Cogeneration Company's SCR system is considered a  
Program 3 process, both release scenarios were evaluated in the offsite  
consequence analysis. 
 
The offsite consequence analysis must include an estimate of the residential  
population within an area potentially affected by the accidental release scenarios.   
This area is defined as a circle with a radius equiv 
alent to the distance the  
release would travel with concentrations at or above the endpoint.  This circle  
also defines the area in which potential environmental receptors must be  
identified. 
 
The worst case release is defined by the U.S. EPA as the total release of the  
contents of the single largest vessel or pipe within 10 minutes.  For liquefied  
gases stored under pressure, the entire contents of the vessel or pipe are  
assumed to be released as a vapor.  A total vapor release is highly unlikely.   
However, this standardized worst case scenario was developed for emergency  
response agencies to use for planning purposes. 
 
An alternative release scenario is a release that is more likely to occur than the  
worst-case release scenario.  For Salinas River Cogeneration Company, the  
alternative release scenario was selected based on the results of the Hazard and  
Operability Study for the ammonia-based SCR process.  The worst credible  
release event with the highest discharge rate wou 
ld potentially have the greatest  
offsite impact.  A failure of the ammonia delivery hose was identified in the  
Hazard and Operability Study as the worst credible release event having the  
highest release rate, and therefore, was chosen as the alternative release  
scenario.     
 
Salinas River Cogeneration Company has analyzed the offsite consequences of  
the worst-case and alternative release.  For the worst-case release scenario, the  
release of 69,960 lbs. of ammonia within 10 minutes, the plume would travel 3.1  
miles at concentrations at or above the endpoint.  Using 1990 Census data, the  
population potentially affected within the worst-case release scenario circle is  
120.  There were no sensitive or environmental receptors within the worst case  
release scenario circle. 
 
Salinas River Cogeneration Company has installed passive and active mitigation  
systems to aid in the control of ammonia, if a release were to occur.  A concrete  
containment wall surrounds the ammonia storage  
and vaporizer system.  A  
release of liquid ammonia could be contained within this area.  The containment  
would limit the ammonia surface area in contact with the ambient air, thereby  
decreasing the rate of volatilization.   
 
The ammonia storage system is also equipped with a water deluge system that  
will spray water onto and around the storage tank.  In the event of a fire, this  
deluge system can be used to cool the tank and help mitigate a temperature  
induced overpressure release. 
 
Although mitigation systems are installed, a specific mitigation factor cannot be  
assigned to the systems.  Therefore, no mitigation factors were included in the  
modeling.  As such, the modeling results should be substantially overstated. 
 
In the alternative release scenario, a failure of the delivery hose was modeled as  
a release of liquefied ammonia stored under pressure.  For a release of 554  
lb/min of anhydrous ammonia, the plume would travel 0.2 mile at concentrations  
at or above the endpoin 
t.  No residences are located within the 0.2 mile area  
around the Salinas River Cogeneration Company facility.  As such, there would  
be no population impacts from the alternative release scenario.  There were also  
no sensitive or environmental receptors within the alternative release scenario  
circle.  
 
The modeling performed as part of this offsite consequence analysis does not  
take into account the use of the remote operated shutoff valves that were  
installed at the ammonia tank.  These isolation valves take approximately 10 to  
15 seconds to fully close and could greatly reduce the impact of a hose failure  
release.  
 
General Accidental Release Prevention Program and Chemical-Specific  
Prevention Steps 
 
A PSM program, which meets the requirements of the general accidental release  
prevention program, has been developed at Salinas River Cogeneration  
Company to address the anhydrous ammonia system.  The PSM program  
includes the following chemical-specific prevention steps: 
 
    W 
ritten process safety information, including information pertaining to the  
hazards of ammonia, the technology of the process, and the equipment in  
the process has been compiled. 
 
    An initial Process Hazard Analysis (PHA) was performed and has been  
updated and revalidated at least every five years. 
 
    Written operating procedures have been developed and implemented, and  
are reviewed at least annually. 
 
    Safe work practices, such as lockout/tagout, confined space entry,  
opening process equipment or piping, and control over entrance into the  
facility have been developed and implemented. 
 
    Each employee involved in operating the ammonia system has received  
initial training and refresher training at least every three years. 
 
    Written mechanical integrity procedures have been established and  
implemented. 
 
    A Management of Change (MOC) program has been developed and  
implemented to address all proposed changes to the ammonia system. 
 
    Pre-startup safety reviews are performed whe 
n a modification is made to  
the ammonia system that is significant enough to require a change in the  
process safety information. 
 
    Audits are conducted at least every three years to evaluate compliance  
with the RMP regulations. 
 
    Incident investigation procedures have been established. 
 
    A written plan of action regarding the implementation of employee  
participation has been developed and implemented. 
 
    Hot work permits are issued for all hot work operations conducted on or  
near the ammonia system. 
 
    A Contractor Safety Policy has been developed and implemented. 
 
To ensure that the general accidental release prevention program and the  
chemical-specific prevention steps are implemented, Salinas River Cogeneration  
Company has assigned overall responsibility for the RMP elements to the  
Executive Director.  The Executive Director has the overall responsibility for the  
development, implementation, and integration of the RMP elements. 
 
Five-Year Accident History 
 
Salinas River  
Cogeneration Company has not had any accidental releases from  
the ammonia-based SCR system that have resulted in deaths, injuries, or  
significant property damage on site, or known offsite deaths, injuries,  
evacuations, sheltering in place, property damage, or environmental damage in  
the last five years. 
 
Emergency Response Program 
 
Salinas River Cogeneration Company has established an emergency action plan  
and a chain of command to respond to emergencies and to notify emergency  
responders when there is a need for a response.  However, an emergency  
response program does not need to be developed for the facility since Salinas  
River Cogeneration Company employees will not respond to accidental releases  
of ammonia, the facility is included in the community emergency response plan,  
and appropriate mechanisms are in place to notify emergency responders. 
 
Planned Changes To Improve Safety 
 
The PHAs were most recently revalidated in March, 1996.  Several changes to  
inspection and of 
floading procedures were recommended based on the PHA  
revalidation.  These changes were implemented by November, 1996. 
 
Through the accidental release prevention program, Salinas River Cogeneration  
Company regularly evaluates the need for any changes to improve safety.   
Currently Salinas River Cogeneration Company does not have any additional  
changes planned to improve safety.
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